June 2000
Vol. 221 No. 6 Feature Article
|
WELL CONTROL
Case histories bring reality to well control training
Louisiana State University, with support from the
Minerals Management Service, used two actual underground blowouts as student teaching /
learning tools
John Rogers Smith, Adam T. Bourgoyne, Jr., Sherif M.
Waly and Eileen B. Hoff, Louisiana State University, Baton Rouge, Louisiana
ase
histories can be used in training to demonstrate the importance of effective well control.
This article focuses on the case history of an underground blowout that occurred during a
trip in the hole on a deep gas well. It reviews the chronological events and emphasizes the
key learnings. Another case history of a near miss due to a small swabbed kick reinforces
some of these learnings. Also described is a case-history-based training simulation which is
designed for students to experience these learnings by making the operational decisions
themselves that might lead to, or prevent, an underground blowout.
Three principal conclusions developed in this presentation
are:
- Case histories can be the basis for a variety of
interactive training methods. These factual experiences establish a sense of reality when
learning well control concepts and methods that cannot be achieved with hypothetical
simulator exercises or example calculations alone.
- The selected case histories strongly reinforce the
importance of preventing, detecting and successfully controlling kicks as the best
approach to preventing and, therefore, controlling blowouts. The importance of seemingly
mundane procedures, such as monitoring pit gain while circulating bottoms up and fill up
during trips, can be demonstrated with training simulations. Concepts normally ignored in
well control training such as the difficulty of conclusively detecting a swabbed-in
kick and the necessity of removing a small, swabbed-in kick on choke can be shown.
- Interactive and simulator training exercises require the
student to make decisions and take corrective actions as symptoms develop, rather than
just practice routine procedures. When these are based on case histories, they provide
valuable "experience" for participants, based on actual events.
Introduction
The ability to successfully prevent blowouts is widely
recognized as a critically important element of any drilling operation. Well control
training is used to give rig-site personnel the practical and theoretical knowledge needed
to develop this ability. However, many preventive / monitoring practices taught in this
training can seem arbitrary, mundane and unnecessarily exacting to trainees.
The case histories described here demonstrate clearly why
careful control and monitoring practices are important for avoiding blowouts, particularly
in deep, high-pressure wells. The Minerals Management Service supported the acquisition of
these case histories, and their adaptation for training purposes, as part of a project on
prevention / control of underground blowouts.
Prevention / control of such blowouts is complicated by
several factors. By definition, an underground blowout is an uncontrolled flow from one
subsurface zone to another. Consequently, there is no opportunity to observe the flow
directly, and diagnosing what is happening in the subsurface is difficult. Even identifying
the occurrence of an underground blowout can be difficult. The consequences are also
uncertain, ranging from insignificant to catastrophic. Usually, the most serious risk is of
the blowout broaching to the seafloor or ground surface and causing a crater, with
consequent damage and danger at the surface.
The industry lacks systematic procedures for analyzing /
controlling underground blowouts. In addition, most conventional well control training
courses allocate less than 5% of course resources to the subject. Some well control manuals
and texts, such as Murchison,1 Abel,2 and Kelly, Bourgoyne and
Holden,3 give some guidelines or example approaches for specific situations, but
not a general method.
Therefore, the industry needs additional training resources
to address the prevention and control of underground blowouts. Such a need was the
justification for using records of previous experiences to create case histories for use as
training exercises, as previously proposed by Bourgoyne and Kelly.4
Overview. A case history of a deep, underground
blowout offshore Texas has previously been used as an effective, interactive, group learning
exercise. 5 A later section of this article will describe briefly how that case
history is being adapted to be an individualized, interactive, programed learning exercise.
Two additional case histories are described herein. The focus will be on an underground
blowout that occurred during a trip in a deep, high-pressure gas well. The important factual
events are presented chronologically, and resultant key learnings are emphasized. Another
case history of a "near miss" reinforces some of these learnings.
These two experiences are the conceptual basis for a
training simulation exercise. Although a complete history match of a major well control
event would be too time consuming for most training, specific situations can be re-created.
These require the trainee to diagnose the situation with the same kind of information that
would exist in reality. Using a simulator allows the trainee to actually implement decisions
rather than just think about their likely results. The exercise and its results from use by
industry professionals are described.
Case history applications. Multiple case histories
have been provided by industry sources for the underground blowout project, and several have
been selected as appropriate for training purposes. In addition, case histories are also
described in some existing well control literature, by Grace,6 Muchison2
and Abel. 3 In general, the examples in literature provide enough information to
make and support a key point, but not to develop a full training exercise. The following two
case histories are the basis for the key learnings and simulation exercise described herein.
C.H. No. 1: Underground Blowout In Deep Gas
Well
The primary well control event reviewed in this article is
an underground blowout that occurred during a trip in a deep gas well. A diagram of the well
at the time it was shut in is shown in Fig. 1.
|
|
Fig. 1. Wellbore diagram showing
conditions when shut in on underground blowout in deep gas well. No. 1: No flow
at surface until far into trip in. Flow out ignored until pits ran over (pit
level detector malfunction). No. 2: SICP = 1,050 psi and builds to 3,400 psi.
Pit gain > 189 bbl indicates at least 200 bbl gas in well and probably lost
circulation. |
|
Chronological description. A deep, offshore gas well
had been drilled to a TD below 22,000 ft MD and 21,000 ft TVD. The objective sand was
reached and found to be gas productive. Several conventional cores were taken and recovered.
A 12.5-lb/gal mud was being used, which provided a 550-psi overbalance. A 9.625-in. liner
was set and cemented just below 13,300 ft and tied back to surface with 10.75-in. pipe. The
leak-off test at the liner shoe was equivalent to 13.7 lb/gal.
A 60-ft core of the objective sand was tripped out of the
hole. Previous trips had caused no problems, and the overbalance should have provided
more-than-adequate trip margin. However, careful monitoring of the trip tank indicated that
the hole had taken 2.5 bbl less than expected. This was not considered a problem, because it
was a relatively small error for such a long trip, and previous, successful trips had
experienced even larger discrepancies. There was no flow from the well after the trip out,
and it was considered successful.
A new bit was picked up, and the trip began uneventfully.
The trip was interrupted at the 9.625-in. casing shoe to slip and cut the drill line. There
was still no indication of flow from the well. The trip was continued to 18,400 ft, where
pit level measurements indicated a gain was occurring. The well was checked for flow and
observed to be "flowing slightly." This was concluded to be thermal expansion of
mud, and the trip was continued.
Tripping continued to about 19,300 ft, but pit level
continued to increase in excess of pipe displacement. The trip was again interrupted, and
the well was shut in. The shut-in drill pipe pressure was 0 psig, but shut-in casing
pressure was 100 psig. The cause of the casing pressure was concluded, by rig personnel, to
be "U-tube effect from out-of-balance mud." Consequently, the trip was again
continued.
Continued pit gain. In reality, a pit gain of at
least 55 bbl had been recorded over the previous 1.5 hr. A quick calculation shows that this
size gas influx would cause 450 to 600-psi loss of hydrostatic head, depending on where it
was in the annulus.
Actual total pit gain was probably larger, given that the
kick had probably occurred much earlier. A larger gain could easily cause the 650-psi loss
of hydrostatic head necessary to cause the 100-psig, shut-in casing pressure. If so, the
well was truly underbalanced when the trip continued, and influx from the formation was
almost certainly occurring.
After tripping to 19,750 ft, the crew concluded that they
should circulate to get the mud back in balance. Although the continuing pit level gain
showed that the well was still flowing at this point, it was not shut in or circulated on
the choke. When circulation began, the total pit gain was at least 73 bbl more than
calculated pipe displacement.
At this point, shut-in casing pressure (SCIP) would probably
have been about 300 psig. If the well had been shut in, it would have been obvious that mud
imbalance was not the problem. An SICP of at least 830 psig could be contained without
losing returns, based on the leak-off test. Therefore, it is likely that the well could have
been killed conventionally at this time.
Circulation continued for about 30 min more. During this
time, the pit level indicator being observed by the operators representative
malfunctioned and showed no gain. The mud logging crew observed that the pit gain was
continuing, but did not advise the operators representative. Afterwards, a review
concluded that a "lack of clear communication" contributed to the "improper"
actions taken by the crew. Another 108 bbl of gain were taken before the pits ran over.
Problem becomes obvious. Circulation continued
another 30 min before rig personnel concluded that the well was really flowing, and it was
shut in. The loss of mud from the pits means that the total pit gain when the well was
finally shut in is unknown, but it was substantially more than the 181 bbl indicated by
mudlogging records at the time the pits overflowed. The SICP was 1,150 psig. If all or most
of the influx was below the 9.625-in. casing shoe, this pressure would result in lost
returns and would initiate an underground blowout.
The drillstring was almost 3,000 ft off bottom. Stripping
was begun to get the bit closer to TD to allow for attempting a conventional well kill.
After stripping eight stands into the hole, SICP had reached 3,400 psig. The cause for this
increase is not certain, but gas migration, pressure buildup after initial shut in and
failure to bleed off pipe displacement would all cause shut-in pressure to increase.
The upper stripper began leaking at this time, allowing an
additional 40-bbl gain. After shutting in to repair the stripper, the SICP was 4,100 psig.
Given these excessive pressures, lost circulation leading to an underground blowout was
almost certainly in progress. An additional complication was that the drillstring became
stuck during the stripper repair with the bit still more than 2,000 ft above TD.
Kill preparations. The seriousness of the situation
was finally obvious. It was clear that conventional control methods were unlikely to
succeed, and preparations were begun to perform an off-bottom kill. The primary focus of
this case history is prevention, but the following summary of kill preparations and
operations is given for completeness.
Engineering calculations indicated that a dynamic kill could
be achieved by pumping several thousand barrels of 13.5-lb/gal mud through the drillstring
and into the loss zone at a rate of about 17 bbl/min. This would require additional mud,
pumps, personnel and other resources to be delivered to the rig. In the meantime, the risk
of a surface blowout could be reduced by minimizing surface pressures.
Surface pressures were reduced by intermittently bullheading
mud into the annulus and pumping mud into the drillstring to keep it at least partially
full. Gas that migrated to the top of the annulus was bled off and replaced with mud during
periods when bullheading was interrupted. Noise logs were run in the drill pipe to confirm
that flow in the annulus was occurring. The outer-casing annulus pressures were monitored
for changes to verify that conditions were not becoming worse. After five days of
preparation and rig-up, the kill operation was ready to begin, and shut-in casing pressure
had been reduced to 1,055 psig.
Kill operation. The final kill plan was to pump
4,000 bbl of 13.5-lb/gal, water-based mud down the drillstring at a rate of 17 bbl/min and a
pressure of at least 6,500 psig. The mud would exit the bit and return up the annulus with
the gas flow to the loss zone just below the 9.625-in. shoe. This rate and density was
calculated to raise pressure at the bit enough to prevent further gas influx. Then, 1,000
bbl of 15.5-lb/gal mud would be pumped and left to fill the annulus between the bit and the
shoe. This would ensure a hydrostatic kill of the well even if gas was left in the well
below the bit.
Three workboats were tied into the rig mud pits to provide a
total of 5,600 bbl of 13.5-lb/gal mud. Another workboat held 2,000 bbl of 15.5-lb/gal mud.
Three turbine-driven pump skids provided 4,000 hydraulic hp for the large-volume,
high-pressure pumping job. Engineers had not only designed the procedure, but had also
predicted the expected pressure-vs.-rate response throughout the job and provided criteria
for determining whether the job was succeeding and should be continued.
The kill operation began by pumping the 13.5-lb/gal mud at 3
bbl/min and staging up to 17 bbl/min to allow verification that hydraulic predictions were
correct. Initial pump pressure at 17 bbl/min was 6,000 psig. As mud began to fill the
annulus, this pressure increased to 6,900 psig. A steady-state condition of 6,800 psig at
16.3 bbl/min was achieved after pumping about 700 bbl. This combination indicated that a
dynamic kill had been achieved.
Circulation continued for another 1,000 bbl to help remove
some remaining gas from the open hole and annulus. Then the planned 1,000 bbl of
15.5-lb/gal, was pumped at a final rate / pressure of 14 bpm and 5,350 psig. Success of the
kill operation was confirmed by running noise and temperature logs to verify that downhole
flow had ceased.
C.H. No. 1 Analysis And Key Learnings
There are several important learnings that can be drawn from
this experience. These relate to the causes of kicks, detection, reaction to unconfirmed
kick indicators and control of severe well control problems.
Key learning No. 1. The actual cause of the initial
gas influx into this well is not known. The operator concluded that one, or both, of the
following could have caused the initial kick that proved so hard to detect conclusively.
- Swabbing on the trip out. Although the indicated 2.5 bbl
swabbed was less than on some other trips, even this small volume could have caused the
well to go underbalanced when it migrated, or was circulated, to within 1,000 ft of
surface. A significant increase in trip gas measured on the last previous trip is
indicative that some minor swabbing may have occurred during that trip as well.
- A 60-ft core was cut prior to the trip. Gas volume in the
volume of formation drilled would have been about 0.6 bbl at bottomhole conditions. Even
this tiny volume could theoretically cause the well to go underbalanced if it were brought
to within 200 ft of the surface as a single bubble. Bottoms up had not been circulated
prior to the trip out, and a share of this gas would have been present in the core.
Consequently, it is possible that all "drilled gas" remained in the well during
the trip and migrated slowly toward surface.
The key learning is that: A small volume of gas influx can
expand enough to displace mud from the well and cause it to become underbalanced, especially
in a deep well.
Key learnings No. 2. Swabbed-in kicks, or other
kicks taken during a temporary underbalance, can be difficult to detect. In this case, the "kick"
was almost certainly taken during the trip out of the hole, as explained above. It was only
detected after tripping over 18,000 ft back in the hole.
Key learnings are:
- A small-volume gas kick can go undetected while
migrating, until its volume expands enough to unload sufficient mud to initiate flow or
cause a significant trip-tank or pit-level change. The migration is very slow in weighted,
water-based mud.
- The large overbalance, in this case, meant that the gas
influx had to expand to about 55 bbl to cause the well to go underbalanced. Therefore,
flowchecks were negative or inconclusive, even after easily-identified, pit level
indications.
- A negative flowcheck is not proof that no kick was taken
in a well, only that there is no influx occurring currently. This is especially important
to remember during trips.
Key learnings No. 3. Reaction to an unconfirmed
indication of a kick is important. In this case, tripping was continued, and then
circulation initiated, without careful monitoring or evaluation of observed flow, pit-level
and pressure indications. The initial indication of a possible kick was apparently a steady
pit gain in excess of what was expected due to pipe displacement while tripping in the hole.
The minor flow noted at 18,400 ft confirmed the possibility that a kick had been taken.
The increasingly strong indicators that a kick had been
taken continued to be discounted until after a very large influx had occurred. The pit level
increased rapidly after enough mud was displaced to cause the well to be underbalanced. Pit
level increased even more rapidly when circulating, because gas was being brought to surface
and expanding even faster, simultaneous with new influx from the formation.
Key learnings are:
- Questionable kick indications require a cautious
reaction. The primary concerns should be detecting whether a kick has occurred and
maintaining the ability to initiate effective well control procedures.
- The slow increase in pit level and insignificant flow
that occurs while gas is migrating will increase rapidly when the well goes underbalanced.
- Circulation brings gas up faster, increases rate of
pit-level increase and decreases reaction time. Circulating bottoms up to eliminate
unbalanced mud or to check for gas should be done only while carefully monitoring pit
level. The crew must be prepared to shut the well in if additional pit gain is observed.
- If the well is not shut in when it becomes underbalanced,
a new kick will begin rapidly. Postponing shut in until pit gain is large can cause
excessive shut-in pressure, lost returns and risk of an underground blowout. Consequently,
circulating the well on choke is inherently safer than routine circulation if a kick is
suspected.
Key learning No. 4. Delay in reacting properly to
the initial gas kick and the subsequent large kick caused a major underground blowout. A gas
formation with 120 ft of 40-mD sand and a 13,400-psig reservoir pressure was flowing
uncontrolled into another permeable zone almost 8,000 ft shallower An effective kill
procedure required density, volume and rate high enough to overcome this high-rate,
underground flow and ultimately regain hydrostatic control, despite having over 2,000 ft of
open hole below the bit.
The key learning is that well control for underground
blowouts and off-bottom conditions requires special procedures not typically addressed in
conventional training. Nevertheless, even a severe loss of control can be corrected with a
properly designed and executed operation.
C.H. No. 2: Near Miss Due To Small Swabbed
Kick
Near misses can also provide a basis for case history-based
learning exercises. This case history is based on one of the authors personal
experience with a small kick that was apparently swabbed-in during a trip out of a deep gas
well. This kick did not result in an underground blowout. However, the well had previously
experienced lost returns, and underground blowouts had been experienced in previous wells in
the area. Consequently, although it was successfully controlled, it is considered to have
been a near miss.
The significance of this case is that it developed in a
similar manner to the previous case, but the cause of the kick is somewhat better documented
and understood. The kick was identified just as the crew was beginning to run a production
liner, and the kick can be concluded to have been caused by the trip out of the hole. A
summary of the experience is described in the following paragraphs. Fig. 2 is a wellbore
sketch indicating the general configuration of this well during the trip out of the hole.
|
|
Fig. 2. Wellbore diagram of near miss
due to swabbed kick. |
|
The well had been drilled to the objective TD below 18,000
ft. After correcting lost returns experienced at TD, it was logged, and a cement plug was
set below 17,500 ft to isolate the lost-circulation zone near TD from shallower, potentially
productive intervals in the open hole. The cement plug was dressed off, the well was
circulated clean with 18.5-lb/gal mud and a trip out was made to run a production liner.
Fill-up volumes were monitored throughout the trip, which
was judged to be routine except for two factors. First, the trip was made somewhat faster
than most previous trips. Second, a 4-bbl "gain" had been noted while laying down
drill collars. The gain was believed to have been caused by floor-washing water spilling
into the trip tank. The well was checked and found not to be flowing.
Preparations were then made to run the 7-in. production
liner, and there was no additional pit gain during this time. However, excess displacement
while running the liner was noted almost immediately. Running was halted temporarily, and
flowchecks were made on two occasions in the first few stands. No flow was observed, and
running continued. "Auto-fill" float equipment was being used to minimize surge
pressures that could have re-initiated lost returns and was thought to be a possible cause
of the fill-up discrepancies.
The remainder of the liner, and 15 stands of drill pipe were
run, as the well was observed to finally be flowing. Having all of the liner in the hole and
drill pipe opposite the BOP stack allowed the well to be shut in. Shut-in drill pipe and
casing pressures were equal at just above 900 psig.
The decision was made to strip the liner in the hole to
enable circulation closer to the likely kick zones. The float equipment was activated so
that it would prevent flow up the drill pipe, and stripping commenced. Ten stands were
stripped before the annular preventer element failed. The well was shut in on the pipe rams,
and the element was replaced. Stripping then continued to about 17,000 ft, where the liner
became stuck. The well was killed conventionally at that depth, and the liner was cemented
successfully.
A maximum pressure of about 1,400 psig was encountered
during stripping. Gas and saltwater-cut mud were circulated out during the kill, but in
smaller volumes than expected. A large amount of mud had been lost during the stripping
operations; apparently, this was equivalent to bullheading a significant fraction of the
kick fluids back into the formations in the open hole.
Analysis / Key Learnings From Swabbed Kick
The precise cause of this kick has never been determined.
Most likely, it resulted from a small, swabbed-in kick at the beginning of the trip. This
conclusion is based on: the trip being faster than previous trips, occurrence of balling and
swabbing on previous trips, "gain" observed while laying down drill collars and
the common occurrence of incorrect hole fill-ups observed on the first few stands pulled.
Although this last possibility is not documented for this trip, it was experienced on
earlier trips; it has been simulated and demonstrated as a feasible explanation for the
actual sequence of events.
The seemingly-late reaction to the kick indicators was still
quick enough to prevent the excessive pit gain and excessive shut-in pressures experienced
in the previous case history. The rig personnels acknowledgment that a kick had
occurred and readiness to initiate stripping before flow became excessive were important to
their success. The low formation permeability and combination of water and gas production
made their challenge easier.
The key learnings are similar to the previous case history:
- A very small volume of gas influx can go undetected while
migrating, until its volume expands enough to unload enough mud to cause a significant pit
gain or to initiate flow.
- Shutting in as soon as practical and stripping in the
hole allowed relatively conventional control of an off-bottom kick taken during a trip.
Simulation-Based Learning Exercises
A simulator training exercise has been developed using a
situation analogous to the second case history described above. It is intended to
demonstrate how a small, swabbed-in kick can be very difficult to detect, but can develop
into a blowout if ignored for too long. The scenario is also representative of the kick that
caused the problem in the first case history. The exercise is implemented on stand-alone,
PC-based, well-control, training / simulation software.
|
"The training exercise begins by advising students that they have just
arrived on the rig for a crew change. A trip from TD has just begun, and the third
stand is being pulled." |
|
|
How the training works. The training exercise begins
by advising students that they have just arrived on the rig for a crew change. A trip from
TD has just begun, and the third stand is being pulled. The floorhand monitoring the
continuous-fill trip tank has advised that the hole has taken at least two barrels less mud
to fill than calculated. The supervisor they are relieving has just requested that the trip
be postponed and the well watched for flow.
The students must then perform the flowcheck and decide what
to do next. They should not be told that the well had kicked. They should have the same
uncertainty about the meaning of a small volume discrepancy that they would have in a real
situation.
There are a number of alternative actions the students might
take after observing that there is no flow. Some of the possible reactions are:
- Assume this is the effect of a slug falling, and continue
tripping out.
- Assume the lack of fill-up volume is in fact a kick, and
shut the well in to begin circulating out on the choke.
- Attempt to circulate bottoms up with the bit nearly 300
ft above TD.
- Trip in to TD and circulate bottoms up.
- Leave the well as-is, and watch for any evidence of flow
over some set time.
There are additional, various reactions that might be taken
as the students observe the results of their decision. In any case, careful observation will
eventually demonstrate that a kick has been taken.
Training objective. A major objective of this
exercise is to allow the student to reach the conclusion that there is a kick in the well
independently of confirmation by the instructor. This shows that the presence of a small
kick is almost undetectable initially. As the kick migrates, it will expand. The expansion
is very slow while the kick is migrating in the lower section of a deep well, and the
resulting pit gain is too slow to detect. As the kick reaches the upper portion of the well,
the gradual expansion will have resulted in a larger kick volume. The hydrostatic pressure
at the kick will also be changing proportionately faster, so the kick will be expanding more
rapidly even if the migration velocity is the same.
The more-rapid expansion, loss of hydrostatic head due to
the kick volume resulting in a formation influx, or the combination of both will eventually
result in detectable flow and significant pit gain at surface. If identified quickly enough,
the well can still be shut in and controlled. In the case of the "near miss,"
control was regained fairly quickly. In the "deep underground blowout," it was
misjudged for too long, and the underground blowout occurred essentially as soon as the well
was shut in. However, this was still less dangerous than a surface blowout.
Results of training. The training exercise has given
similar results. It has been used in training more than 20 industry professionals. Their
first reaction is usually to ask the instructor what to do. Because they are in a well
control training course, they expect to have to shut the well in. Asked what they would do
in the field if this were a real case, the reaction is usually to carefully check for flow.
After identifying that there is no flow, there will
typically be one of two reactions. One is to trip back to bottom to circulate bottoms up and
check whether a kick was taken. The other is to continue tripping out of the hole. In either
case, essentially nothing happens to indicate whether a kick is present until the gas has
reached the upper few-thousand feet of the well.
The simulation is of a 3-bbl, swabbed-in kick in a 10,000-ft
well. This was selected to simulate the effect of an even-smaller kick that had migrated to
10,000 ft in a deeper well. The 10,000-ft depth was chosen to reduce the total amount of
simulation time. A wellbore diagram for the simulation is shown in Fig. 3. In actual case
histories, the flow was not detectable until after more than 10 hr of migration.
|
|
Fig. 3. Wellbore diagram for training
simulations. |
|
The simulation demonstrates this effect with a much shorter
period of apparent inaction. Even so, one student team had an experience similar to the deep
underground blowout. Apparently, the lack of any "action" during the early part of
the simulation caused them to become distracted. They missed the initial indications that
the well was flowing and that a pit gain was occurring. The pits eventually overflowed,
causing the simulator screen to flash red, and the simulator was "frozen" to
prevent the simulation from blowing out.
Fig. 4 is an example of the subsurface pressures and pit
gain vs. time recorded for a sequence of events like this that ultimately simulates a
blowout. Note that once, the well becomes underbalanced, it unloads more quickly and
wellbore pressures drop rapidly. The reduced pressure causes an increased rate of flow into
the well. In the simulation, several hours are required for the gas to migrate to a depth of
about 2,200 ft, where it has expanded enough to cause a 10-bbl-total pit gain. Within 10
min, the kick has migrated to about 1,300 ft and expanded enough that the well becomes
underbalanced, and the formation begins to flow. Within another 10 min, the gas reaches the
surface.
|
Fig. 4. Pressures and pit gain for
simulation of uncontrolled, swabbed-in kick. |
|
Key learnings. The most common reaction by industry
participants is to use precautions commonly taken in the field. They trip back to bottom and
begin circulating bottoms up. Again, there is very little "action" initially.
However, the 69 min required to circulate bottoms up only requires 7 min at X10 on the
simulator. So, the kick reaches the upper portion of the well fairly quickly.
A gradually-increasing pit gain warns an observant team that
there may indeed be a kick in the well. Depending on how rapidly the team detects this, a
flow can usually be observed if the pumps are stopped. If so, the well is shut in, and
conventional well control is begun. Given that the well already contains kill-weight mud,
the drillers method can be used to remove the kick and re-fill the well with mud.
This approach is usually successful and fairly uneventful.
The casing pressures and pit gain observed during this procedure re-confirm that a kick had
been taken. Fig. 5 is an example of the pressures and pit gain vs. time recorded in a
simulation of this sequence of events.
|
Fig. 5. Pressures and pit gain for
simulation of effective shut in and kill of swabbed-in kick. |
|
Three key learnings can be experienced using this exercise:
- A small kick in an overbalanced well, as from swabbing,
is very hard to detect. After the simulation, calculations of hydrostatic pressures in the
well can be done to demonstrate why.
- When circulating bottoms up to check for a kick, or when
continuing a trip after an inconclusive kick indication, the critical crew responsibility
is to keep monitoring kick-detection parameters. If a small gas kick is present,
eventually it will cause enough pit gain to be detected.
- The period of time during which the kick can be
identified and shut in safely may only be a few minutes. Failure to react rapidly and
appropriately can cause complete loss of control.
Given that many kicks occur on trips and that some
result in serious surface or underground blowouts this is an important learning
exercise to supplement more-routine exercises, where the kick is taken while drilling and is
more easily detected.
Other Training Exercises
The original training exercise developed for this project
was based on a deep, underground flow offshore Texas. It has been used as a successful group
learning exercise for almost 100 industry professionals and rig personnel, and more than 50
petroleum engineering students. The Petroleum Engineering and Industrial Engineering
departments at LSU have also initiated a cooperative effort to adapt the original,
interactive group-training exercise as a programed learning exercise for individuals. This
exercise is being implemented on PC software. It would allow an individual to make decisions
by selecting from a predefined list of alternatives and then to be advised of the result.
Wellbore sketches are used to clarify well conditions
resulting from previous decisions. Key learnings are emphasized as they become evident in
the results of the students decisions, or as results of the actual decisions made in
the field are explained.
Another new training module has just been started to
simulate the "deep underground flow." It is intended to re-create major decision
points and actions that resulted in the underground blowout and which ultimately brought it
back under control. Re-creating the entire case history in a single simulation would be time
consuming, even at the X10 maximum speed of the simulator. However, specific point-in-time
situations that occurred during the case history allow simulation of subsequent events, as
well as alternative courses of action that might have been taken. Each such situation then
becomes a separate learning exercise within the context of the actual events that occurred.
This allows key lessons from the case history to be learned in a "hands-on,"
experiential manner by students operating the simulator.
Note: This article was prepared from
the paper, "Case histories bring reality to well control training," presented by
the authors at the IADC Well Control Conference of the Americas, Houston, Texas, Aug. 2526,
1999.
Acknowledgment
The authors appreciate the support and encouragement from
the Minerals Management Service for this project. They also thank LSU for its support and
permission to publish. This work would not have been possible without the information
provided by operators and their drilling personnel; it is greatly appreciated. Colin Leach
is also acknowledged for sharing his understanding of swabbed-in kicks.
Literature Cited
- Murchison, W., Well control for the man on the rig,
1980.
- Abel, L. W., et al., Firefighting and blowout control,
Wild Well Control Inc., Spring, Texas, 1994.
- Kelly, O. A., A. T. Bourgoyne, Jr. and W. R. Holden, et
al., Blowout prevention, a short course, Louisiana State University, Baton Rouge,
Louisiana, 1992.
- Bourgoyne, A. T., Jr. and O. A. Kelly, "Development
of improved procedures for detecting and handling underground blowouts in a marine
environment An overview," LSU/MMS Well Control Workshop, Baton Rouge,
Louisiana, March 3031, 1994.
- Smith, J. R. and A. T. Bourgoyne, Jr., "Case
history-based training for control and prevention of underground blowouts," paper SPE
38605, SPE Annual Technical Conference, San Antonio, Texas, Oct. 58, 1997.
- Grace, R. D., "Analyzing and understanding the
underground blowout," paper IADC/SPE 27501, Dallas, Texas, Feb. 1518, 1994.
The authors
John Rogers Smith, a
Campanile Professor and assistant professor in PE at Louisiana State University, holds a BS
in EE from the University of Texas and MS and PhD degrees in PE from LSU. He previously
worked for Amoco Production Co. He is currently an SPE distinguished lecturer on deep
drilling and a member of AADE, ASME and SPE.
Adam T. (Ted) Bourgoyne, Jr. received
BS and MS Degrees in PE at LSU and a PhD in PE at the University of Texas at Austin. He
began his career as a senior systems engineer with Conoco. In 1971 he joined LSU as an
Assistant Professor. Since then, he has worked in the undergraduate, graduate, and
continuing education programs of LSUs PE Department. He served as Chairman of the
Department from 1977 to 1983 and as Acting Dean of Engineering from 1985 to 1987. Until his
retirement from LSU in December 1999, he was the Campanile Professor of the Craft &
Hawkins Department of PE and Dean of the College of Engineering. He has been active in
blowout prevention and guided development of a research / training well facility at LSU.
Sherif M. Waly earned
a BS degree in systems / biomedical engineering in 1981 and MS degrees in biomedical and
industrial engineering in 1988. He received a PhD from the University of Miami in 1994. He
joined the Industrial and Manufacturing Systems Engineering department of LSU in 1995. He
was previously a research associate and instructor at the University of Miami. His research
areas include industrial human factors, occupational biomechanics and safety engineering.
Mr. Waly has authored / co-authored more than 70 articles / papers.
Eileen Hoff is a
graduate student at Louisiana State University where she is completing work on her
dissertation in engineering science. Her current research focuses are on ergonomic aspects
of oil production / safety training. She has BS and MS degrees in industrial engineering.
|