BSEE releases panel investigation report into subsea jumper leak


WASHINGTON -- The Bureau of Safety and Environmental Enforcement (BSEE) has released the panel investigation report on the May 11, 2016 subsea jumper leak on a platform operated by Shell Offshore, Inc. The leak from Green Canyon Block 248 occurred on Subsea Well No. 4, resulting in an estimated release of 1,926 bbl of oil.

The BSEE investigation panel concluded that the loss of containment in the Glider subsea system was caused by the ductile tensile overload fracture of the Load Limiting Joint of the Glider No. 4 jumper. The ductile tensile overload fracture was caused by the bending loads imposed as a result of the partial burial of the Glider No. 4 jumper and subsequent subsiding of the subsea sled No. 2.

The panel recommends when drilling the riserless portion of a subsea well in the vicinity of other subsea infrastructure (i.e. pipelines, sleds, subsea wells, etc.), operators need to ensure the resulting drill cuttings and cement are not adversely affecting or posing additional risks to existing subsea infrastructure.

To read more about the panel investigation, the full report can be found here.

A Safety Alert has been sent to offshore operators and can be viewed here.


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